It was suggested to me to post on this site and hope a gentleman named rodbolt responds. 2001 250 ox66 pair. Port motor started acting up a week ago. On the way in from a trip the motors had been running for 1.5 hours at 4300 rpm and instantly the port motor dropped to 3000-3400 rpm giving it more gas gave no response.The symptons are erratic but it will always do it within 10 minutes of running sometimes when you are just getting up on plane or after a few miles of being on plane.The motors idle perfect. Either it will bog trying to get on plane around 3000-3400 and surge back and forth until it "catches" and then run fine for a few miles and then drop down to anywhere from 2800-3800 until it "catches" again. The other day it bogged at 3000-3400 for a mile or so and I watched the flow meter and it held steady like the motor was running at 4300(14 gph) Since then I have replaced vst filters-no signs of problems, checked twice the fuel rail pressure both times while it was surging it read 38psi and never fluctuated, checked voltage at high pressure pump it held steady at 12.7 volts, swapped fuel pickup at primer ball, bypassed big racor filters/flow sensor and 3 way fuel valve, replaced all fuel lines except hoses from tanks(including hose inside rigging tube), installed new lp pumps and swapped the entire motor mounted fuel canister/lp pumps and associated hoses up to the vst tank, swapped the vst tanks, swapped rails and installed new fuel lines at the rail, swapped the injectors. Also, checked with the winky blinky(no errors), cleaned/swapped the O2 sensor, swapped crank position sensor,installed new tps(and adjusted-I have test harness) and swapped the tps, swappped the atmospheric pressure sensor, swapped the cdi unit twice(with all coils,wires),installed new spark plugs and swapped the spark plugs, disconnected the intake temp sensor from both motors and they both idled poorly and ran rough(I could not figure out how to remove them to swap), swapped the knock sensor, swapped the high pressure rectifier, swapped neutral cutoff switch, swapped the stator and flywheel, swapped the main engine harness, swapped the wire harness from the injectors to the main harness, swapped the 10 pin plug at the keyswitch, used a short 10 pin plug and a keyswitch to bypass the ignition cable going from the keyswitch to the main engine harness. After numerous test runs this motor defies logic nothing has worked. I bought these motors new and have kept up the maintenence to a high level. Help!!