scout-j-m
Chief Petty Officer
- Joined
- Jul 31, 2009
- Messages
- 642
I picked up the subject motor late last summer for really cheap. Figured I'd fix it or strip it and sell the good parts. Luckily it had great compression but the CDI box was shot. I waited probably 3-4 months for the by far cheapest one online to get back in stock and got it installed and now have excellent spark. I lightly cleaned the carb and replaced the impeller and the little 9.8 fired right up. However, nothing came from the pisser nor any other exhaust location above the water line in the barrel I ran it in. Got my IR thermometer and restarted it and the temp on head was getting crazy hot so I shut it down and pulled the lower unit. Submerged the lower in a bucket and put the driveshaft in the chuck of my drill and was able to verify that the water pump was working great. I blew compressed air both up the water tube and back into the pisser fitting on the block/head. When blown into the head the air was exiting the exhaust through the leg but when blown up the water tube it felt and sounded almost completely plugged. I assume there is a rubber grommet of some sorts where the water tube meets the powerhead. I also assume I have to pull the powerhead to replace. Am I on the right path here? Is it relatively easy to pull the powerhead on these model motors? It looks pretty simple but this is my first time working on this model.