bullsnot
Seaman
- Joined
- Aug 22, 2012
- Messages
- 60
Last fall I lost an impeller and boat overheated. Engine is a 2000 5.7L Mag MPI. After compression test and leak down tests I decided to replace the heads. Swapped stock ones for brand new stock heads. I reused the roller lifters and push rods. I followed the manual. Started at cylinder 1 TDC. Tightened until lash gone, then another 1 full turn on each valve listed for that position in the manual. Then moved the engine to cylinder 6 TDC and tightened the appropriate cylinders in the same fashion.
I fired it up and it ran rough and had valve train noise. Never could fix it. I pulled the valve covers off an discovered 3 bent push rods. Other than DIY mechanic error is there anything else that could cause this?
I fired it up and it ran rough and had valve train noise. Never could fix it. I pulled the valve covers off an discovered 3 bent push rods. Other than DIY mechanic error is there anything else that could cause this?