Need some help here guys. I have a 2003 Tritoon with a Vortec 4.3 I/O. Bought it used last fall and have had it out about a dozen times running about 200 gallon thru it. Last weekend, on Saturday, it ran like a top as usual. On Sunday, unloaded it off the trailer and was idling in the marina waiting on my wife to return from parking truck. And all of a sudden I could hear lifter noise that got increasingly louder. I thought first off that it might have a stuck lifter, but giving it a bit of gas made it worse. Then it quit. Luckily I wasn't out in the middle of no-where and got it back on the trailer easily.
Long story as short as I can! I took the engine out on Monday. Tore into it last night. Found the middle exhaust rocker (opposite starter) just laying on top of the tower. Bolt still in rocker but backed all the way out. I took the pushrod out and checked straightness. It was ok.
To back up a bit. After getting the engine out, I discovered it was a remaufactured unit. Nicely done, couldn't tell from looking at back of engine. Hard to see in the hull anyway. But ran fine the times we had it out.
Now for the problem at hand. I rotated the crank to get that cylinder to TDC compression and torqued the bolt (Yes mine has a bolt, not a stud and nut - roller cam) down to the recommended 22ft pds. What I noticed was the rocker pushed the valve down ever so slightly, about .125. Rotating the crank didn't help relax the lifter. SO I broke loose the intake rocker on the same cylinder. Keep in mind I checked the pushrod and it spun like it should. No pressure. The valve did not move when rocker was released. BUT when I tightened the rocker back up, same issue. It pushed the valve down about .125" . So I moved to another exhaust valve same thing...What gives. Why are the lifters not relaxing. What am I doing wrong?
I plan on taking the heads off tonight and checking the cylinders to make sure there is no other damage. It doesn't appear that there is anything else wrong other than the backed off rocker. Maybe it wasn't tightened correctly when remanufactured. The gas filter said 08-2008, so I'm assuming it was probably changed the same time the engine was installed. SO it has ran fine for about 2 years.
Sorry for such a long post, but I've searched these threads and there is not much info on the newer Vortec 4.3 heads.... Is there anything that would make the rocker bolt back out other than it wasn't tight to start with? The threads are perfect, not stripped in any way. At least 1" thread engagement. I'm stumped
Any thoughts? Maybe the rest of the teardown will show something. Hopefully not, though. Hoping this repair is only gonna cost me a gasket set! 
Long story as short as I can! I took the engine out on Monday. Tore into it last night. Found the middle exhaust rocker (opposite starter) just laying on top of the tower. Bolt still in rocker but backed all the way out. I took the pushrod out and checked straightness. It was ok.
To back up a bit. After getting the engine out, I discovered it was a remaufactured unit. Nicely done, couldn't tell from looking at back of engine. Hard to see in the hull anyway. But ran fine the times we had it out.
Now for the problem at hand. I rotated the crank to get that cylinder to TDC compression and torqued the bolt (Yes mine has a bolt, not a stud and nut - roller cam) down to the recommended 22ft pds. What I noticed was the rocker pushed the valve down ever so slightly, about .125. Rotating the crank didn't help relax the lifter. SO I broke loose the intake rocker on the same cylinder. Keep in mind I checked the pushrod and it spun like it should. No pressure. The valve did not move when rocker was released. BUT when I tightened the rocker back up, same issue. It pushed the valve down about .125" . So I moved to another exhaust valve same thing...What gives. Why are the lifters not relaxing. What am I doing wrong?
I plan on taking the heads off tonight and checking the cylinders to make sure there is no other damage. It doesn't appear that there is anything else wrong other than the backed off rocker. Maybe it wasn't tightened correctly when remanufactured. The gas filter said 08-2008, so I'm assuming it was probably changed the same time the engine was installed. SO it has ran fine for about 2 years.
Sorry for such a long post, but I've searched these threads and there is not much info on the newer Vortec 4.3 heads.... Is there anything that would make the rocker bolt back out other than it wasn't tight to start with? The threads are perfect, not stripped in any way. At least 1" thread engagement. I'm stumped