rch105
Cadet
- Joined
- May 17, 2011
- Messages
- 10
2001 185BR Sea Ray, 4.3L, all stock. Low hours (under 250) Always fresh water.
We've had the boat since new and I've winterized it the same way for each winter season. No issues when we I winterized it last September. Fresh oil filter, oil, and fuel/water separator to start this season off.
Went on vacation, July 14th, and upon start up it, seemed to take a little longer to run. Upon pulling from the dock area power was bad. Couldn't get to plane. Went about 300 yards and made a loop back to launch site as she was starting to labor. As I approached dock I saw the bilge was running and it was a chocolate milkshake coming out the bilge. Shut down immediately. Pulled cover to find the milkshake was spewed all over the top of engine, etc. It appears to have forced it's way back up the hoses connected to each side of the arrestor. Thoughts anyone? I've been researching it and I have a few reasons for this but would appreciate anyone's input. TIA!
We've had the boat since new and I've winterized it the same way for each winter season. No issues when we I winterized it last September. Fresh oil filter, oil, and fuel/water separator to start this season off.
Went on vacation, July 14th, and upon start up it, seemed to take a little longer to run. Upon pulling from the dock area power was bad. Couldn't get to plane. Went about 300 yards and made a loop back to launch site as she was starting to labor. As I approached dock I saw the bilge was running and it was a chocolate milkshake coming out the bilge. Shut down immediately. Pulled cover to find the milkshake was spewed all over the top of engine, etc. It appears to have forced it's way back up the hoses connected to each side of the arrestor. Thoughts anyone? I've been researching it and I have a few reasons for this but would appreciate anyone's input. TIA!