I recently purchased a 1966 Johnson FD20C. I replaced the two fuel hoses to and from fuel pump, oil return line with clear tubing, fuel pump, new needle and seat, new float, and new packing washers on low speed adjustment needle (old packing washers deteriorated.) Took out for test run and after warming engine I fine tuned low sped adjustment turning needle in until engine started to cough at low idle then backed needle out until engine ran smooth. I noticed if I slowed idle speed is lowered slower than start/idle speed gas/oil leaking out out of exhaust. Also noticed at low idle oil return line has more flow than higher speeds. Is this normal for these old motors? Motor pushes 1448 flat with approx 500 pounds including me and gear 23 mph (checked with gps.)