JDRains
Cadet
- Joined
- Aug 12, 2017
- Messages
- 19
I was given a 71 glastron with a 74 Mercury 1500 last month. Actually rode in the boat the last time it was in the water 21 years ago and it would peg the 45 mph speedometer. The motor itself was a fresh rebuild.
I've had to clean 21 years of dirt, dust and varmits even though the boat was in covered storage and rewired it. I cleaned all of the motor wire harness connections, pulled the coil wire to the distributor and cleaned the coil end, pulled the distributor cap off the trigger and lightly cleaned the rotor and the contact points in the cap. New trigger timing belt was installed. Pulled plugs to discover they were brand new, liberally fogged each cyclinder with penetrating oil and let sit for a couple of days before turning over with a battery. I mixed super unleaded @ 50:1 added a half can of Seafoam and some marine stabil. After sitting 21 years it actually fired up and ran after heavy pumping on the priming bulb. I noticed no water coming out of the pee hole so I shut it off.
Definitely going to have all the seals in he lower unit replaced as well as the water pump and pump housing. Before starting it up again. So far it hasn't ran long enough to get warm. I suspect maybe dirt dobbers have got in the lower unit ss to the reason for no water out of the pee hole.
Right now it's a toss up as to whether I have the carburetors rebuilt with lower unit or wait until I can actually run it waith confimed water flow.. Oh, I did swap out 22 prop to a 20.
I welcome any suggestions on what I can expect out of this resurrected old Tower of Power.
I've had to clean 21 years of dirt, dust and varmits even though the boat was in covered storage and rewired it. I cleaned all of the motor wire harness connections, pulled the coil wire to the distributor and cleaned the coil end, pulled the distributor cap off the trigger and lightly cleaned the rotor and the contact points in the cap. New trigger timing belt was installed. Pulled plugs to discover they were brand new, liberally fogged each cyclinder with penetrating oil and let sit for a couple of days before turning over with a battery. I mixed super unleaded @ 50:1 added a half can of Seafoam and some marine stabil. After sitting 21 years it actually fired up and ran after heavy pumping on the priming bulb. I noticed no water coming out of the pee hole so I shut it off.
Definitely going to have all the seals in he lower unit replaced as well as the water pump and pump housing. Before starting it up again. So far it hasn't ran long enough to get warm. I suspect maybe dirt dobbers have got in the lower unit ss to the reason for no water out of the pee hole.
Right now it's a toss up as to whether I have the carburetors rebuilt with lower unit or wait until I can actually run it waith confimed water flow.. Oh, I did swap out 22 prop to a 20.
I welcome any suggestions on what I can expect out of this resurrected old Tower of Power.