H60Chopperdr
Cadet
- Joined
- Jan 1, 2012
- Messages
- 9
Hi all,
New to the site. I'll try to make this as brief as possible. Motor developed a knock noise last year. Decided to run it to it's death as I have twin engines and the other can bring me home. Well, knocking stbd engine lost most power and decided it had enough. I ordered a new base engine and swapped over the external parts. Pulled old engine apart and found one piston had a 1/4" x 1/16" spot worn away on outer edge. Combustion blew past the worn away edge and annihilated the rings and upper 1/2 outer piston (ring groves and lands) and skirt surface. This of course caused blow by and fouled plugs but that is not the issue. My issue is this. Now that I have the new engine about ready to install I am worried this can happen again. I suspect detonation. What could have caused the detonation? I used good fuel with Seafoam. It was not an octane problem. Is my timing off? It is a TBI with what I believe is TB V ignition. The distributor does not hold the ECM or KSM. I think my KSM is mounted to the left riser elbow. Could it be a bad KS? Any advice is great. I don't want a repeat of this $3K shenanigan.
Additional info:
About 600 hrs on motor
Exhaust manifolds were nearly corroded shut (put new ones on new engine and port engine)
One other question. New base engine has a much larger threaded hole on the LH lower block where the knock sensor was mounted on old engine. Now my knock sensor won't fit. Why? How do I remedy this?
Thanks.
New to the site. I'll try to make this as brief as possible. Motor developed a knock noise last year. Decided to run it to it's death as I have twin engines and the other can bring me home. Well, knocking stbd engine lost most power and decided it had enough. I ordered a new base engine and swapped over the external parts. Pulled old engine apart and found one piston had a 1/4" x 1/16" spot worn away on outer edge. Combustion blew past the worn away edge and annihilated the rings and upper 1/2 outer piston (ring groves and lands) and skirt surface. This of course caused blow by and fouled plugs but that is not the issue. My issue is this. Now that I have the new engine about ready to install I am worried this can happen again. I suspect detonation. What could have caused the detonation? I used good fuel with Seafoam. It was not an octane problem. Is my timing off? It is a TBI with what I believe is TB V ignition. The distributor does not hold the ECM or KSM. I think my KSM is mounted to the left riser elbow. Could it be a bad KS? Any advice is great. I don't want a repeat of this $3K shenanigan.
Additional info:
About 600 hrs on motor
Exhaust manifolds were nearly corroded shut (put new ones on new engine and port engine)
One other question. New base engine has a much larger threaded hole on the LH lower block where the knock sensor was mounted on old engine. Now my knock sensor won't fit. Why? How do I remedy this?
Thanks.