Caddy_Kid
Petty Officer 2nd Class
- Joined
- Nov 18, 2005
- Messages
- 113
I have a 1965 Merc Mark 1000 in line 6, double coil ignition. 100 PSI compression in each hole, new plugs (Champion J4C's). Here is a list of events:<br /><br />Bought boat motor and trailer this winter, owner deminstrated motor.<br /><br />Boat has origional built in tanks. One was half full of 10+ year old gas, other dry, neither hooked up. Drained and plumbed tanks. Both had hard varnish on all the inside surfaces.<br /><br />Had some motor work done when I found one plug was stripped out. Fired it up a couple times in a garbage can and it ran great, idled fine, nice and smooth while attached to a new carry on tank (didnt want the boat full of gas when I was working on it in the garage).<br /><br />Took it to the lake 3 weeks ago for a test run (on the built in tanks, no carry on) and it did fantastic. Smooth idle, quick throttle response, no dead spot, 4500 RPM WOT. Idled at 1000 RPM which I was going to take down before I took it out again. Took it home (didnt run the engine out of fuel, didnt have a shut off valve yet).<br /><br />Bought a new lower pitch prop. Took it out a week after the first run (last friday). Idled at 800 RPM at the dock (didnt touch the idle from the first time so it should have been 1000). Hit the throttle and it bogged and shuttered. Would only hit 2500 RPM and ran like crap. Would run on high idle anywhere from 2500 up to over 3500 RPM with the idle lever in the fully open position. Go up, come down, go up, come down. Switching tanks from side to side didnt help. Took it back home.<br /><br />Checked plugs, all look fine. Filled the carbs with Sea Foam cleaner and let it sit over night. Drained the carbs this afternoon, turned the built in tanks on and fired it up. Same as at the lake. It would run great up to 3500, then bomb down to 2500 or lower, then slowly climb back. Adjusting the idle mixture screws would make it run faster and a bit better, but then it wouldnt idle as they were screwed most of the way out at that point. Squeezed the primer bulb, thinking maybe it was starving for fuel because of bad pumps, plugged line, etc which dropped the RPM and tried to flood it on the first squeeze.<br /><br />Switched back to the carry on with brand new gas, oil (50:1) and mid-grade fuel. No change.<br /><br />Just took the filters off, soaked them in acetone and blew them out. No visable clogs there. Cleaned the idle adjustment screws which also looked clean.<br /><br />Before I take the carbs apart, what am I missing here? Sorry its so long winded, but figured more specifics might help. My guess is that the old varnish is now disolving in the new gas and its somehow messing with the motor. I figured switching to new gas and tank would help, but it didnt. Thanks.