Re: 73 lightwin tuning problem
Here is the long time in coming update (sorry to those whom ofered advise previously):
I fixed the cord, so the non stop pulling can continue.
Now The motor would not start at all. ( things are going down hill)
The motor is a 4106d weedless 4 hp
So here goes. The coils were cracked and I could see burn marks, so I replaced them, as well as the condensers. One set of points was poorly alined, so I changed them as well. The end result is that I have strong spark on a motor that still won't start.
I went through the carb again, and it looks clean. The reed valves look good. I changed the fuel twice. There is fuel coming out of the fuel pump, and when I pull the high speed needle out after a few pulls, gas drains out of the bowl.
The compression is great. Both cylinders are well over 100.
I took the cover off the exhaust port that is underneath the the starter cord, and found that the gasket was leaking coolant (water) into the exhaust chamber next to the cylinders. There was emulsified oil in there. There was also a hint of it on the plugs
It was late, and the parts store was not open, so I made a temp. gasket of 411. No Dice. It will fire some times, for a second then die.
My new plan.
Get the real gasket for that exhaust port.
Is it possible that the timing is so messed up that it won't start? Is it possible that this emulsified oil in the exhaust is getting into the cylinder, and stoppingg combustion? where can I look to see if there is water getting into the intake side?
Thanks for your time