Cherokee-Runabout
Petty Officer 3rd Class
- Joined
- May 30, 2012
- Messages
- 90
A few days ago I was worried that my motor was overheating after it had cut out on me one day .I went forward and pulled the lower to inspect/ flush water tube and inspect impeller. In order to remove the impeller, it seemed stuck on, i oulled the drive shaft through the housing. Everything seemed to check out, impeller showed little wear and seemed to retain a good deal of elasticity as blades almost completely straightened out. I then hooked up a piece of tubing to the water tube and connected other end to garden hose nozzle on "jet" setting to flush out anything that may have been blocking the tube. I then reassembled everything and noticed that the shift lever on side of cowling was up a little higher for neutral than it was originally and I felt that this was a difference in where I had tightened the linkage and wasn't concerned because shifter rod seemed as though it was shifting between forward and neutral. I then noticed that the prop would not spin when in either neutral or forward. ( Shouldn't it spin freely in neutral?) I tried to run it and shift into forward after bokting everything up. No luck... I then tried to adjust shift back to normal positions. Once again it felt as though the gears we're engaging but once again no rotation in prop . I'm going to pull lower again and see if I can get it to function. Any suggestions on what may be the cause? Also any ideas on what may cause engine to cut out after 15 minutes of running at wot and emit white vapor ( unsure of smoke or steam) from lower (maybe carbon )? It was in the mid to upper 80s that day and I was running the motor against a decent flow. Thanks again!