- Joined
- Jul 18, 2011
- Messages
- 18,137
I have 980 hours on my twin Mercruiser 7.4 LX MPI engines. They are going to lap 1,000 next season, as I average 40 hours per year, since buying the boat in 2012. . . 2013 being our first season with it on the water.
I have not done a compression test in a couple of years, so I wanted to do one at this point just to see where things stand. 1,000 hours is when you start thinking about rebuilding engines, etc.
I got a new compression tester (Innova model 3612), and one thing I noticed is that the check valve is right at the fitting for the spark plug hole, which my other tester did not have. The check valve was after a short adapter hose, which would lower the compression #'s somewhat. I seemed to get pretty good #'s with this gauge . . . not sure how much is the actual differences in the gauges (old vs. new) vs. the improved design of the new gauge.
Another thing that I did was to run a decarb a La SeaFoam before doing the tests. I used a method that I learned from Mischief Managed , which I think works particularly well for MPI engines.
I mixed up a 50/50 mix of Seafoam and gasoline in an aux. tank. Brought the engines up to temperature, then switched the fuel to the 50/50 mix. After the mix had a chance to get into the fuel rail, I unplugged the ignition wire on one of the cylinders and let the engine run on 7 cylinders for 2 minutes. Then I re-plugged that ignition wire and went to the next cylinder's wire unplugging and re-plugging until all cylinders had been run for 2 mins getting the seafoam mix without firing.
I then switched back to the regular fuel and let the engine purge the remaining seafoam mix. I'm not sure how much this helped, but it sure seemed like a clever seafoam solution for an MPI engine.
After I ran the engines for about 10 additional minutes on regular fuel, I did the compression tests. Here is what I got . . .
PORT ENGINE
1 - 149
3 - 140
5 - 131
7 - 149
2 - 160
4 - 138
6 - 147
8 - 153
STARBOARD ENGINE
1 - 147
3 - 146
5 - 134
7 - 150
2 - 156
4 - 132
6 - 145
8 - 148
A couple of low cylinder on each engine, but overall i'm pleasantly surprised with the results. Looks like I can hold off on a rebuild for a while.
Thoughts ??? :noidea:
I have not done a compression test in a couple of years, so I wanted to do one at this point just to see where things stand. 1,000 hours is when you start thinking about rebuilding engines, etc.
I got a new compression tester (Innova model 3612), and one thing I noticed is that the check valve is right at the fitting for the spark plug hole, which my other tester did not have. The check valve was after a short adapter hose, which would lower the compression #'s somewhat. I seemed to get pretty good #'s with this gauge . . . not sure how much is the actual differences in the gauges (old vs. new) vs. the improved design of the new gauge.
Another thing that I did was to run a decarb a La SeaFoam before doing the tests. I used a method that I learned from Mischief Managed , which I think works particularly well for MPI engines.
I mixed up a 50/50 mix of Seafoam and gasoline in an aux. tank. Brought the engines up to temperature, then switched the fuel to the 50/50 mix. After the mix had a chance to get into the fuel rail, I unplugged the ignition wire on one of the cylinders and let the engine run on 7 cylinders for 2 minutes. Then I re-plugged that ignition wire and went to the next cylinder's wire unplugging and re-plugging until all cylinders had been run for 2 mins getting the seafoam mix without firing.
I then switched back to the regular fuel and let the engine purge the remaining seafoam mix. I'm not sure how much this helped, but it sure seemed like a clever seafoam solution for an MPI engine.
After I ran the engines for about 10 additional minutes on regular fuel, I did the compression tests. Here is what I got . . .
PORT ENGINE
1 - 149
3 - 140
5 - 131
7 - 149
2 - 160
4 - 138
6 - 147
8 - 153
STARBOARD ENGINE
1 - 147
3 - 146
5 - 134
7 - 150
2 - 156
4 - 132
6 - 145
8 - 148
A couple of low cylinder on each engine, but overall i'm pleasantly surprised with the results. Looks like I can hold off on a rebuild for a while.
Thoughts ??? :noidea: