Boat was running fine at the start of the season. I noticed a little dripping in the lower front of the engine suggesting a water pump needing to be replaced. Got the parts and replaced water pump. Getting to the three hex bolts I did turn the motor over several times to get to the hex bolts. I did this with both belts off and I’m now wondering if I affected the timing because now it is running rough. Runs fine at start up full throttle but then starts to bog and sputter out. Pull throttle back to 3-3500 rpm’s and you can feel the power go in and out. Almost like it’s not getting enough gas. Still runs but several times that same process repeats itself. Hatch was opened and it rained while working on it and wondered if water made its way in the carb. Wondering if Seafoam would cure it? So several possibilities going on here. Anyone here experience the same type thing going on?
Thanks,
Brad
Thanks,
Brad