I have a 1987 VIP 17 ft Fish and Ski pushed by a 1987 125 hp Force. The motor has always seemed to run pretty well for what we needed although never above about 4300 rpm wot with a 19 p prop and just me in the boat. It pulls a skier but could not get a wakeboarder up a few weekends ago. I found a reconditioned 15 p prop and bought it thinking this is the fix for the low rpm and thus quicker hole shot and less time to plane, etc. Well, things didn't turn out as planned. Almost no change in rpm or in planing speed or hole shot. I read where the jet size may be changed, but we are only at 365 ft. I do think it runs too rich because there is raw fuel dripping from the <br />bowl(s) and it would not start Saturday am until I removed the cowl. I had both carbs rebuilt last year about this time when I bought the boat. I plan to do a decarb on it tomorrow as I do not know when this was last done. Could this help the problem if it is a stuck float and what improvements could I expect from this process? What other things should I do (compression check, spark check etc.)? Thank you for wading through my rambling and for all the good advice. <br /><br />Thanks again,