satleecher
Recruit
- Joined
- Sep 11, 2008
- Messages
- 5
I bought it, asked a pensioned person to prepare the motor working, had at least 3 years of non running hours (costed me about 500 US$, but still worth it, I think). I boated for about 15 hours, last week everything ok, but I noticed that the stationary was higher then usual (choke closed). Today with my family... starting conditions as usual...that is..open choke. pull twice..he will then say 'whroaaahhhh.....' and stops (normal), close choke, pull twice and working. Also today, and again I noticed higher stationary...pulled on mercontrol in shift and off on stationary to exit the habour....normally then push throttle further for the sound and power....then.... blup-blup... motor stopped. Shift in N, pull and start without problem, in shift again, still ok, throttle further...end again. This I tried several times no succes. We boated back on stationary and ended the trip.... I have a theory that maybe the motor after three years is now 'cleaned' and that air/fuel is the problem. So too much fuel or too less air when opening the throttle. But I have NO CLUE where to adjust. Or could the timing be shifted? Who can help me. I am afraid to go the pensione person... he like to charge.... I expect it's a small item. Thanks for any help. Dag en bedankt (like we say in dutch).