nola mike
Vice Admiral
- Joined
- Apr 22, 2009
- Messages
- 5,524
Beautiful weekend, decided to try to get the boat running before september this season 
I had a spare outdrive from my donor boat that I decided to put on this year, appeared to be in better shape than my other one, and I started low speed overheating at the end of last season. I changed the u-joints (managed to break a tab off the retainer getting the old ones out) and water pump/housing/seal. Couldn't get the halves back together, looked up into the housing and saw the remains of that #$!% shaft o-ring. Removed, cleaned, couldn't get together again, realized that somehow that lower shift seal got buggered. I for some reason had a spare on hand, so back in business. Alignment unchanged since last time the drive was pulled. Not 2 finger loose, but not terrible.
Jumped the fuel pump for a few seconds, and the thing fired up on literally the first crank. I don't think that's ever happened first thing in the spring ever to me.
Ran for about 45 minutes on muffs. No sign of overheat, no leaking, oil looks good. Cool, hopefully survived my first winterization.
@Scott06 kept on pestering me to check the timing advance last season. I tried, but my cheap timing light crapped out after 2k rpm or so. Set the idle using dwell meter for rpm instead of the gauge, realized my timing was only 5' BTDC. I doubt that this is enough to make a difference, but we'll see. I'll test it to make sure it's advancing correctly as well once I get on the water.
Hopefully I'll have time to pretty up the wiring, hook up the electronics, and clean the damn thing this year!
I had a spare outdrive from my donor boat that I decided to put on this year, appeared to be in better shape than my other one, and I started low speed overheating at the end of last season. I changed the u-joints (managed to break a tab off the retainer getting the old ones out) and water pump/housing/seal. Couldn't get the halves back together, looked up into the housing and saw the remains of that #$!% shaft o-ring. Removed, cleaned, couldn't get together again, realized that somehow that lower shift seal got buggered. I for some reason had a spare on hand, so back in business. Alignment unchanged since last time the drive was pulled. Not 2 finger loose, but not terrible.
Jumped the fuel pump for a few seconds, and the thing fired up on literally the first crank. I don't think that's ever happened first thing in the spring ever to me.
Ran for about 45 minutes on muffs. No sign of overheat, no leaking, oil looks good. Cool, hopefully survived my first winterization.
@Scott06 kept on pestering me to check the timing advance last season. I tried, but my cheap timing light crapped out after 2k rpm or so. Set the idle using dwell meter for rpm instead of the gauge, realized my timing was only 5' BTDC. I doubt that this is enough to make a difference, but we'll see. I'll test it to make sure it's advancing correctly as well once I get on the water.
Hopefully I'll have time to pretty up the wiring, hook up the electronics, and clean the damn thing this year!