Re: Hints when replacing lower unit oil seals on MK 1000?
Its put back together now. Replaced the shift shaft bushing, two oil seals in the bottom of the water pump housing, the one seal in the top, installed a new impeller and water pump rebuild kit (gaskets, O ring, wear plate, water tube guide). The drive shaft had some rust on it where the lower water pump housing oil seals are, so I cleaned it off with a dremel and packed the space between the seals with grease. I hope it can seal with the pitting that occurred.
Had to make a spanner socket that was deep and big enough to take the shift shaft bushing out. I used a piece of steel pipe and a steel pipe connector. Cut and ground the connector so that it had two "ears" (using the seam on the connector for strength as well as an easy way to find center) that fit in the shift shaft bushing, attached it to the pipe, and had to use a big pipe wrench on the pipe to get it to come out. It was really galled in there. Re-installed with some grease on the threads. I included a picture.
Made sure to loosen the shift shaft one turn at a time, then tap the shaft back down, just in case removing it walked it up. Had no problems! Got it all put back togeather and it still shifts like it should.
Also fixed the lack of a reverse lock out. Some previous owner had installed the lock out actuator arm into the lower unit incorrectly. It wasnt in the hole in a nylon bushing that keep the shift shaft and arm in the propper alignment. Easy enough to get wrong, as I did it once, which is how I learned where it should go! Got it in the right hole and adjusted, and it works great now.
So all in all it was very successful. I wouldnt have a problem doing it in the future on another motor. Also purchased a lower unit oil pump. It threads into the lower unit drain hole and pumps from an oil bottle. Real time saver, and only $10.
UPDATE: Took the boat to the lake this weekend and after a good day at the lake, the lower unit oil is nice and amber, just like when I put it in! Before the repair, it would be mustard yellow after just a couple hours. So it worked!