j5wentworth
Cadet
- Joined
- Aug 20, 2012
- Messages
- 18
So, I inherited a 1964 Evinrude 18 HP Fastwin that needed some work. I found out it was leaking gear oil so I decided to break it all down and i replaced all seals, gear case head assembly, shift seal bushing / o ring, impeller , etc. I have two main concerns now that it's been partially re-assembled. Everything went back together smoothly without any forcing.
Problem 1:
With the lower unit re-assembled but unattached from the upper , it takes a pretty good amount of force to turn the prop / drive shaft while in gear - either forward or reverse. It seems like too much resistance to me, but I didn't check it before to compare. Neutral is perfectly fine with no resistance. I noticed no wear on any of the gears and dog clutch had minimal wear. The only thing I could think of is that the new gear case head assembly was slightly longer than the original, but it was the same part # when I ordered it and it fit the same. Thoughts on anything I did wrong or need to look for?
Problem 2:
When I dropped the lower unit, I left the shift linkage in neutral and loosened the lower of the two shift linkage screws to remove. When I reassembled and tried to fit the lower to the upper, I found the shift linkage was too short now. I tried installing with it in forward and reverse and it's still too short.
So, what in the world am I doing wrong? I had none of these issues before , so I'm sure I messed something up, but not sure what.
Thanks for the help!
Problem 1:
With the lower unit re-assembled but unattached from the upper , it takes a pretty good amount of force to turn the prop / drive shaft while in gear - either forward or reverse. It seems like too much resistance to me, but I didn't check it before to compare. Neutral is perfectly fine with no resistance. I noticed no wear on any of the gears and dog clutch had minimal wear. The only thing I could think of is that the new gear case head assembly was slightly longer than the original, but it was the same part # when I ordered it and it fit the same. Thoughts on anything I did wrong or need to look for?
Problem 2:
When I dropped the lower unit, I left the shift linkage in neutral and loosened the lower of the two shift linkage screws to remove. When I reassembled and tried to fit the lower to the upper, I found the shift linkage was too short now. I tried installing with it in forward and reverse and it's still too short.
So, what in the world am I doing wrong? I had none of these issues before , so I'm sure I messed something up, but not sure what.
Thanks for the help!