I am getting the engine ready to remove and found a clue that may point to the reason the coupler failed. When I looked closer at the top mounting nut on the forward mounts as I began to remove the lags it did not look right. I grabbed it and it was finger tight on the left side and was just above the lock washer on the right side. I am so disappointed that I did not at least touch all that when I was looking it over pre-purchase. This boat has tall freeboard and the caverns back there are too deep for me to reach anything unless I take the seatback out first, but I had it out to do the filter and could have discovered this before it failed, grrrrr.
Who knows who or what got interrupted that led to the top nuts not being tightened into the lock washer, sigh.
So, with the engine being able to move up some each time the boat grabbed air and came down hard was affecting the coupler. Probably.
I will start a new thread if I run into any problems with the alignment.
Later....
Who knows who or what got interrupted that led to the top nuts not being tightened into the lock washer, sigh.
So, with the engine being able to move up some each time the boat grabbed air and came down hard was affecting the coupler. Probably.
I will start a new thread if I run into any problems with the alignment.
Later....