CamaroMan
Petty Officer 1st Class
- Joined
- Mar 18, 2016
- Messages
- 330
Originally wrote to Joe Reeves on his website but I see he is finished so just pasting all that down here 
Hi joe - thanks for offering this service. I have a customer with a 85 (i think) 200, been thru alot of head scratching with it.
Replaced stator, trigger, and both packs from CDI - initially one pack had a bias of 22k ohms, both are now equal.
Carbs cleaned, idling at 10-12 atdc which I think is right, did carbs 5 months back - WH22 carbs, triple checked the front facing jet arrangement. Compression 130-140 on all 6, powerhead was rebuilt apparently 2 years ago..
We just replaced the reed block with chris carson fibreglass reeds after suspecting the reeds, similar issue but it does seem a little better, the tach sits around 850 and now and then spits out exhaust with a burny eye gas.. which im wondering is a weak or intermittent weak spark issue perhaps?
New gas, new plugs, new quicksilver oil mixed 50:1 -
At my wits end with this thing-
Thanks! I hope i have included enough info - If I left anything out please ask -
Here is a 30s video of it idling, you can hear it dip now and then and blow a little thru exhaust by the prop- this is about as good as I can get it, 900 rpms at about 10-12 ATDC-
https://www.youtube.com/watch?v=tw5u_lb08D4
Im going to do a spark gap test again - i have noticed #3 shows a few cuts in the timing light strobe possibly indicating a pack or trigger or coil issue but I have been up and down the chain doing all the cdi tests over and over and got good DVA results all over..
Remote control short shaft
Hi joe - thanks for offering this service. I have a customer with a 85 (i think) 200, been thru alot of head scratching with it.
Replaced stator, trigger, and both packs from CDI - initially one pack had a bias of 22k ohms, both are now equal.
Carbs cleaned, idling at 10-12 atdc which I think is right, did carbs 5 months back - WH22 carbs, triple checked the front facing jet arrangement. Compression 130-140 on all 6, powerhead was rebuilt apparently 2 years ago..
We just replaced the reed block with chris carson fibreglass reeds after suspecting the reeds, similar issue but it does seem a little better, the tach sits around 850 and now and then spits out exhaust with a burny eye gas.. which im wondering is a weak or intermittent weak spark issue perhaps?
New gas, new plugs, new quicksilver oil mixed 50:1 -
At my wits end with this thing-
Thanks! I hope i have included enough info - If I left anything out please ask -
Here is a 30s video of it idling, you can hear it dip now and then and blow a little thru exhaust by the prop- this is about as good as I can get it, 900 rpms at about 10-12 ATDC-
https://www.youtube.com/watch?v=tw5u_lb08D4
Im going to do a spark gap test again - i have noticed #3 shows a few cuts in the timing light strobe possibly indicating a pack or trigger or coil issue but I have been up and down the chain doing all the cdi tests over and over and got good DVA results all over..
Remote control short shaft