The compression test results seemed good to me. My results were 171, 182, 181, 171 psi from cylinder 1-4. Others have commented my gauge may be inaccurate as the numbers are higher than expected. Nonetheless the results are all relatively consistent, which I believe is the desired outcome of a compression test. I replaced the fuel filter, which didn't look too bad, but i noticed the paint on the inside of the filter housing was peeling, so i cleaned the housing prior to reinstallation. The tank has fresh fuel. The carb has been removed and sprayed with carb cleaner (not a full bath treatment, but looked good and clean), also replaced the small filter in the carb too which was quite clean, save for a few small pieces of debris in it. I was been having issues hard starting, but was able to resolve that with additional cleaning of the TKS passage in the carb which dislodged a small piece of debris - fires up reliably now. The motor itself seems to run very good. I'm actually hitting too high of rpm's getting out of the hole, it was about 5300 today (which I didn't do for long as I realize that's not a good thing to push). Base timing is set at 2* btdc, idle total advance at 15*, BUT total advance at 3000+ rpm is only 22* (4* too low). If i adjust the distributor position slightly so that base timing is right at 0* TDC (2* advanced from spec), then the idle advance moves up 2* to 17*, and the 3000+ rpm advance also moves up 2* to 24* (which is still 2* too low vs spec although within the +-2* range).