Motor:1974 1150 Inline
Time since rebuild: 15 hours (estimate)
Plugs
ermagap
Compression (1-6):119-120-120-122-120-120
My issue is that yesterday I found out that it was not charging (seperate Issue)when the battery pooped out in the middle of the lake when I tried to start up and move. As it was cranking, I feared that I had flooded the engine, so I pulled plugs to clean it out a bit. When I pulled #2, I saw some light brownish stuff on the plug. It had some water bubbles on it. Not many, but a few small ones, and it looked foamy. So I pulled more plugs and they looked fine. Long story short, I got home and looked into it a bit further. I started with a compression check, thinking if there was a bad gasket, I would have low numbers. Obviously not. Pretty consistent. I then refired the engine and let it run a bit on muffs at warm up RPM. I shut it off and looked again. Now I had the foam on 2 and 3. I switched plug positions and refired. Now I had it on 1, 5 and 2. So I got a fresh can of fuel and ran it from there. Same thing, but different plugs.
The reason for rebuild by the previous owner was an over heated "2 Cylinder and scored cylinder. Pistons are now .015 over I think.
I am wondering if I have a bad batch of gas, or what else could it be? Can someone help?
Time since rebuild: 15 hours (estimate)
Plugs
Compression (1-6):119-120-120-122-120-120
My issue is that yesterday I found out that it was not charging (seperate Issue)when the battery pooped out in the middle of the lake when I tried to start up and move. As it was cranking, I feared that I had flooded the engine, so I pulled plugs to clean it out a bit. When I pulled #2, I saw some light brownish stuff on the plug. It had some water bubbles on it. Not many, but a few small ones, and it looked foamy. So I pulled more plugs and they looked fine. Long story short, I got home and looked into it a bit further. I started with a compression check, thinking if there was a bad gasket, I would have low numbers. Obviously not. Pretty consistent. I then refired the engine and let it run a bit on muffs at warm up RPM. I shut it off and looked again. Now I had the foam on 2 and 3. I switched plug positions and refired. Now I had it on 1, 5 and 2. So I got a fresh can of fuel and ran it from there. Same thing, but different plugs.
The reason for rebuild by the previous owner was an over heated "2 Cylinder and scored cylinder. Pistons are now .015 over I think.
I am wondering if I have a bad batch of gas, or what else could it be? Can someone help?