Don Hansen
Petty Officer 1st Class
- Joined
- Sep 17, 2007
- Messages
- 230
Re: Will this work with my 4 hp
I held off from telling the whole story about my 4 hp but here goes. My 1970 4 hp with many many hours on it developed a noisy connecting rod plus was getting real tired. I saw a 1974 power head for sale on Ebay that the seller claimed had low hours and since power heads from 1970 to 1977 have the same part number, I ordered it. When I got it I was surprised that I could still see, by looking through the spark plug holes, the cross hatch on the cylinder wall. It was then I noticed that this power head also had a loose rod. Since it was getting close to my trip to Canada I thought I would take a chance and rebuild it when I got home. Well, it lasted one hour before the rod let loose and put that hole in the block. Since I could tell that the power head had never been taken apart and was truly low hours here's what I think happened. In 1974 someone bought a new 4 hp but noticed after a few hours that it was making a noise. Instead of repairing the original power head they replaced it with a new one. The bad power head sat on a shelf for all those years until someone decided they could sell it on Ebay. I paid $125 each for the power head, the new crankshaft, and the connecting rod but hopefully I'm getting a like new motor out of it.
DLH
you can get a welder to fix that with aluminum of the correct thickness, But it might be cheaper to buy a used one on e-bay, the salvage yards listed here on iboats.
I held off from telling the whole story about my 4 hp but here goes. My 1970 4 hp with many many hours on it developed a noisy connecting rod plus was getting real tired. I saw a 1974 power head for sale on Ebay that the seller claimed had low hours and since power heads from 1970 to 1977 have the same part number, I ordered it. When I got it I was surprised that I could still see, by looking through the spark plug holes, the cross hatch on the cylinder wall. It was then I noticed that this power head also had a loose rod. Since it was getting close to my trip to Canada I thought I would take a chance and rebuild it when I got home. Well, it lasted one hour before the rod let loose and put that hole in the block. Since I could tell that the power head had never been taken apart and was truly low hours here's what I think happened. In 1974 someone bought a new 4 hp but noticed after a few hours that it was making a noise. Instead of repairing the original power head they replaced it with a new one. The bad power head sat on a shelf for all those years until someone decided they could sell it on Ebay. I paid $125 each for the power head, the new crankshaft, and the connecting rod but hopefully I'm getting a like new motor out of it.
DLH