cobbcfi
Petty Officer 2nd Class
- Joined
- Jun 30, 2010
- Messages
- 150
I have posted many times about my 225 but after the powerhead change 2 years ago the lower gearcase ran dry like my relationship with the girl that had the truck to tow it.. Replaced the gearcase last week but when I did I missed the water pickup and torqued it down.. Overheated for sure but we only went 100yds at low idle thrust.. Engine shut down and wouldnt fire back up.. I sprinkled ( NOT soaked the engine with a garden hose to try to cool it off) and we pulled the gearcase off dockside and made sure the water pickup lined up.. Idles fine now with a great pee out the back and still have 100/1 oil gas/mix from original break-in 2 years ago so it stayed lubed but got really hot.. Now it does fine slow idle and high idle cruise but after 2k/3k RPMS it has a random BANG BANG BANG and thens runs great for 30 seconds and the BANG BANG BANG comes back.. I was told water in the fuel makes the engine do that.. I disconnected a lot of wires/plugs and hit them with an air compressor, made it run a lot better but still has that random BANG.. It's not a misfire (I guess it is to some extent) but I'm at a loss here.. In-line fuel filter is dark (I assume 100-1) mix still in there and maybe a crapped out fuel/water separator??
I guess my question after this whole dissertation Is, what is cause the loud BANGS while under way??
Thanks again for all the help over the years..
I guess my question after this whole dissertation Is, what is cause the loud BANGS while under way??
Thanks again for all the help over the years..
Last edited: