aquasport1998
Cadet
- Joined
- Apr 13, 2010
- Messages
- 23
Hey guys. I have a '98 Merc 200 saltwater that is having a couple of issues this season. Getting her ready this year, noticed that I had a fuel leak at one of the connectors in the motor. Tightened the compression fitting and it closed the leak up. Ran fine for the first couple of times out, then started laboring at around 3500 rpm, wouldn't get on plane unless I moved passengers to front of boat. (Didn't tell my sister that she had packed on a few pounds...didn't feel like swimming that day).
Noticed that bulb was not firming up when I primed, but motor would start. Replaced the bulb and the inline fuel filter. Also noticed a crack in the fuel line running to the bulb, so trimmed it and reinstalled the bulb.
Same problem. bulb doesn't get hard, but motor will start. Runs fine on muffs and in N at the dock. When I pull away from dock and try to get her up to speed, she does well up to about 2000 rpm now. Then labors hard and wont climb above that. In N she revs up to above 3500 rpm before I back her down ( I know not to do that often).
Wondering if I should replace the fuel line and the fuel/water separator. Any thing else to think about before I take her to the Mechanic. Carbs were cleaned 2 years ago. Read somewhere that it might be a power pack issue. How to test?
Thanks ahead for any help.
Noticed that bulb was not firming up when I primed, but motor would start. Replaced the bulb and the inline fuel filter. Also noticed a crack in the fuel line running to the bulb, so trimmed it and reinstalled the bulb.
Same problem. bulb doesn't get hard, but motor will start. Runs fine on muffs and in N at the dock. When I pull away from dock and try to get her up to speed, she does well up to about 2000 rpm now. Then labors hard and wont climb above that. In N she revs up to above 3500 rpm before I back her down ( I know not to do that often).
Wondering if I should replace the fuel line and the fuel/water separator. Any thing else to think about before I take her to the Mechanic. Carbs were cleaned 2 years ago. Read somewhere that it might be a power pack issue. How to test?
Thanks ahead for any help.