Solomon_Man
Petty Officer 2nd Class
- Joined
- Sep 16, 2009
- Messages
- 110
Re: 1955 25Hp Big Twin....
All,
I hooked up a hose to see if the top end is not clogged. Its clear and water flowed out as expected.
I noticed the following;
Around the shift rod (at least from what I can tell) a large amount of water was flowing down the rod. (No leaks at my connection as I doubled clamped it)
Also there appeared to be a man-made hole (maybe drilled/machined/foundried) just below the exhaust on the interior portion of the exhaust housing which allowed a decent amount of water to flow on the insde of the exhaust housing.
I am not sure if any of the above is normal.....?
I also tried to remove the copper tube to put into the water pump for a test. I cannot just pull it out as my diagram shows it is "fitted" with a some type fitting. Trust me this morning I tried pulling it. Does this seem correct?
I was thinking I could try some pipe as a replacement for the copper tubing for the waterpump/lower unit testing.
So I was going to hook my drill to the driveshaft and see if it could pump. Unfortunately, the drive shaft is about 5/8....my largest drill is a 1/2...Looking for ideas on this one....Any have any suggestions?
Thanks,
Chris
All,
I hooked up a hose to see if the top end is not clogged. Its clear and water flowed out as expected.
I noticed the following;
Around the shift rod (at least from what I can tell) a large amount of water was flowing down the rod. (No leaks at my connection as I doubled clamped it)
Also there appeared to be a man-made hole (maybe drilled/machined/foundried) just below the exhaust on the interior portion of the exhaust housing which allowed a decent amount of water to flow on the insde of the exhaust housing.
I am not sure if any of the above is normal.....?
I also tried to remove the copper tube to put into the water pump for a test. I cannot just pull it out as my diagram shows it is "fitted" with a some type fitting. Trust me this morning I tried pulling it. Does this seem correct?
I was thinking I could try some pipe as a replacement for the copper tubing for the waterpump/lower unit testing.
So I was going to hook my drill to the driveshaft and see if it could pump. Unfortunately, the drive shaft is about 5/8....my largest drill is a 1/2...Looking for ideas on this one....Any have any suggestions?
Thanks,
Chris